So I wanted to give a bit of an update,
Little jeep was running well, then I kept having low boost code popping up and going into limp mode. Looked at the vacuum actuator arm and it did move freely when vacuum was removed but it still kept throwing the code. So parked the jeep and removed the turbo and then was able to get the turbine exhaust housing off...boy that sucker was stuck on too.
Once apart, a bunch of hard rock like carbon fell out and the vanes would only move through half of its full range of motion. So fully took it and had the housing and vanes assemblies glass media blasted an now the vanes move fully open to fully close. I did have to replace the 3 screws that hold down the vanes as they sheared off during removal. Replaced them with stainless steel allen head screws and blue locked tight them in.
Since I had the turbo apart I though this would be a good time to attempt a rebuild of the turbo and replace the journal bearing and seals. Note: did not have any play in the turbo shaft, it was for more of preventative maintenance. Got the rebuild kit from G-pop and started the disassemble. Well needless to say I must not have been paying very close attention during the disassembly process cuz every time I tried to put the turbo back together, either the exhaust shield on the turbine side would be lose and rattle inside the housing, the compressor wheel would bind on the compressor housing or if i tighten the compressor wheel to much it would not spin...
So a quick message was sent out to Blackbird innovations (dieselguy_86) and he said he could help me rebuild it properly and rebalance the assembly. Sent the turbo to him and hopefully I'll get it back next week.
While I wait for turbo to return, I went ahead and ordered all new motor mounts and transmission mounts. Passenger side mount was easy to do since I didn't have the turbo in the way and had it replaced in 15 mins. However the driver side mount did not want to cooperate. I can't seem to get the damm bottom nut off. Used both a deep 18mm socket and shallow socket with universal joints and extension and I couldn't break the nut free. Even tried to air impact gun and the only thing I was able to do was spin the socket on the nut...
So before I did any real damage decided to call it quits and not mess with it anymore. Went ahead and changed out the trans mount. Note: I swapped over the heat shield from the old mount to the new mount to protect the rubber from exhaust heat. The original mounts were the original with 175K miles on them. The trans mount was covered in trans fluid and oil and the rubber was a bit squishy. I think I know were the oil leak is coming from but have to investigate the trans leak at a later date.
More to come...